Difference between revisions of "Tales from the Severn Valley"

From SVR Wiki
Jump to: navigation, search
(confirm details of minor derailment)
m (further minor update)
Line 3: Line 3:
  
 
==Minor Derailments==
 
==Minor Derailments==
In summer 1977 the SVR experienced two minor derailments in quick succession.  The first was unusual for the reason it happened; 45110’s rear coupled driving wheels were derailed by a piece of coal in Bridgnorth yard!  The second was notable for the manner in which it was resolved; 47383 got ‘in the dirt’ at Highley while on standby duty.  Once the crew had packed the wheels with some handy fishplates that were lying about, the conductor-driver of a passing train left his own locomotive, boarded the casualty, drove it back onto the rails, re-joined his own train and left without any delay to the passenger service.
+
In summer 1977 the SVR experienced two minor derailments in quick succession.  The first was unusual for the reason it happened; 45110’s rear coupled driving wheels were derailed by a piece of coal in Bridgnorth yard!  The second was notable for the manner in which it was resolved; 47383 got ‘in the dirt’ at Highley while on standby duty.  Once the crew had packed the wheels with some handy fishplates that were lying about, a Driver/Director passing on 80079 left his own locomotive, boarded the casualty, drove it back onto the rails, re-joined his own train and left without any delay to the passenger service.
  
 
==Llanfairpwllgwyngyllgogerychwyrndrobwllllantysiliogogogoch aka Highley==
 
==Llanfairpwllgwyngyllgogerychwyrndrobwllllantysiliogogogoch aka Highley==

Revision as of 17:01, 1 February 2015

A page for sundry stories from the history of the SVRSevern Valley Railway. Mostly taken from SVRSevern Valley Railway News, but feel free to add your own reminiscences.


Minor Derailments

In summer 1977 the SVRSevern Valley Railway experienced two minor derailments in quick succession. The first was unusual for the reason it happened; 45110’s rear coupled driving wheels were derailed by a piece of coal in Bridgnorth yard! The second was notable for the manner in which it was resolved; 47383 got ‘in the dirt’ at Highley while on standby duty. Once the crew had packed the wheels with some handy fishplates that were lying about, a Driver/Director passing on 80079 left his own locomotive, boarded the casualty, drove it back onto the rails, re-joined his own train and left without any delay to the passenger service.

Llanfairpwllgwyngyllgogerychwyrndrobwllllantysiliogogogoch aka Highley

During 1982, passengers between Arley and Hampton Loade were surprised to find themselves passing Llanfairpwllgwyngyllgogerychwyrndrobwllllantysiliogogogoch. Highley had been renamed for the filming of a TV commercial.

Nesting Thrush floors 3205

In 1983, 3205 failed a Fitness To Run examination for an unlikely reason; a thrush had nested in the cab! The locomotive returned to service once the fledglings had flown the nest.

Lady A' steps-in for Clun Castle

Also in 1983, Hunslet 686 The Lady Armaghdale spent 7 weeks at the Birmingham Railway Museum (now Tyseley Locomotive Works) and took place in Tyseley’s celebrations of 75 years as a steam depot. Sunday 5 June was scheduled to be Industrial Steam Day, but Tyseley’s own Peckett was out of action. In an unusual role reversal, ‘Lady A’ hauled passenger services all day while 7029 Clun Castle acted as Depot shunter.

Severn Valley Railway News saves the day

Severn Valley Railway News (the Railway’s quarterly magazine) is not just a good read, it once rescued a railtour! While on an SVRSevern Valley Railway Railtours excursion in April 1984, Class 40 no 40024 failed at Hereford. The fault was diagnosed as a loose contactor causing poor electrical connection. The offending contactor was wedged in place with a copy of SVRSevern Valley Railway News, and the tour continued to Leeds after a 10 minute delay.

See also

The Severn Valley Railway in preservation